[Hobbypower Pixhawk PX4 Flight Controller]
[HKPilot32 Flight Controller] [products]
Arming is failing and I’m down to these messages.
PreArm: Logging failed Frame: QUAD fmuv2 002A0037 3337510B 32343735 ChibiOS: ff603d11 ArduCopter V3.6.3 (63eb66fe) PreArm: Logging failed u-blox 1 HW: 00080000 SW: ROM CORE 3.01 (107888) PreArm: Logging failed PreArm: Hardware safety switch EKF2 IMU1 tilt alignment complete EKF2 IMU0 tilt alignment complete EKF2 IMU1 initial yaw alignment complete EKF2 IMU0 initial yaw alignment complete GPS 1: detected as u-blox at 115200 baud Frame: QUAD fmuv2 002A0037 3337510B 32343735 ChibiOS: ff603d11 ArduCopter V3.6.3 (63eb66fe) Barometer calibration complete Initialising APMThere’s an arm check for logging that had to be disabled. Now arming works.